Please use this identifier to cite or link to this item: http://cmuir.cmu.ac.th/jspui/handle/6653943832/77341
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dc.contributor.authorPatiphat Mueanglueen_US
dc.contributor.authorRungchat Chompu-Inwaien_US
dc.date.accessioned2022-10-16T07:28:26Z-
dc.date.available2022-10-16T07:28:26Z-
dc.date.issued2021-09-15en_US
dc.identifier.issn15517616en_US
dc.identifier.issn0094243Xen_US
dc.identifier.other2-s2.0-85115621944en_US
dc.identifier.other10.1063/5.0063862en_US
dc.identifier.urihttps://www.scopus.com/inward/record.uri?partnerID=HzOxMe3b&scp=85115621944&origin=inwarden_US
dc.identifier.urihttp://cmuir.cmu.ac.th/jspui/handle/6653943832/77341-
dc.description.abstractThe case study company produces jewelry products for export. One of the problems found in its production lines is product defects. The main objective of this research was then to reduce defective products in the case study company production process using Six Sigma Technique. This research was conducted following 5 steps of DMAIC: Define, Measure, Analyze, Improve and Control. The company is giving prior attention to reduce defective products occurring in the top part item manufacturing process, since it is a process that is produced regularly. The Define step aimed to define the scope of the project using Pareto Chart. It was found that the most frequently encountered product defect was hole type. This research then focused on solving the hole type defect problem in the top part item production line. Next, the objective of the Measure step was to evaluate and understand the current state of the process. Key metrics, e.g. percentage of defective product, were studied for comparison with the results after improvement. In addition, the measurement system was analyzed using Attribute Gage Repeatability and Reproducibility technique. Next, the Analyze step aimed to find the root causes of the problem. Root causes of defective product were determined using Process Mapping, Fish Bone Diagram, and Cause and Effect Matrix. The Improve step was aimed at eliminating the root causes of the problem using Design of Experiment Technique. Full Factorial Design of Experiment with 4 factors, each with 2 levels, was conducted to find factors affecting the occurrence of product defects and appropriate conditions of each factor. The factors studied were burning temperature, number of pieces per mold, metal casting temperature and pressure of metal injection. Finally, in the Control phase, the objective was to maintain the conditions of the improvement. Control chart (p chart) and standard operating procedures were developed and used. In conclusion, the research results were able to reduce the hole type defective products from 7.82% to 1.84%.en_US
dc.subjectPhysics and Astronomyen_US
dc.titleDefective product reduction in jewelry part production using six sigma techniqueen_US
dc.typeConference Proceedingen_US
article.title.sourcetitleAIP Conference Proceedingsen_US
article.volume2397en_US
article.stream.affiliationsChiang Mai Universityen_US
Appears in Collections:CMUL: Journal Articles

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