Please use this identifier to cite or link to this item: http://cmuir.cmu.ac.th/jspui/handle/6653943832/74650
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dc.contributor.authorSomkeit Noamnaen_US
dc.contributor.authorTheerapong Thongphunen_US
dc.contributor.authorChalermpon Kongjiten_US
dc.date.accessioned2022-10-16T06:45:48Z-
dc.date.available2022-10-16T06:45:48Z-
dc.date.issued2022-06-01en_US
dc.identifier.issn25869159en_US
dc.identifier.other2-s2.0-85134712514en_US
dc.identifier.other10.11113/aej.V12.16712en_US
dc.identifier.urihttps://www.scopus.com/inward/record.uri?partnerID=HzOxMe3b&scp=85134712514&origin=inwarden_US
dc.identifier.urihttp://cmuir.cmu.ac.th/jspui/handle/6653943832/74650-
dc.description.abstractThe situation of the covid-19 epidemic is a driving force of the global market's demand increase of electronic devices and parts. Entire electronic component manufacturers, especially the transformer manufacturing industry, which is a device that supplies power to many electronic devices, encounters problems in producing products that are unable to keep up with the quickly increasing demand. This research aims to increase the productivity of small transformers by lean approach. The paper depicts processes relevant to improving production processes, reducing waste, and finding unnecessary processes. The method begins with two actions. First, study the current situation in transformer manufacturing of a case study. Second, study the customer order to delivery process using the Value Stream Mapping (VSM) and analyze entire processes of transformer manufacturing to identify standard time by unit work. The main technique is for measuring working time by timing the forward motion with the time measurement method version 2 (MTM-2). The Cause and Effect diagram was displayed with improving guidelines on two operations. First the concept of lean manufacturing was used in principal role, second the ECRS technique (Eliminate, Combine, Rearrange and Simplify) was applied to reduce "waste"as well as to optimize and reduce the manufacturing process of the transformer. The results lead to an increase in the final product per hour from 45 pieces per hour to 75 pieces per hour which increases up to 30% per hour. In addition, the productivity improvements increased the productivity of 3.46 workers per hour to 6.82 per hour (increase of 97.11%) and production time was reduced from 1,109 seconds to 229 seconds (73.04% of productivity).en_US
dc.subjectChemical Engineeringen_US
dc.subjectComputer Scienceen_US
dc.subjectEarth and Planetary Sciencesen_US
dc.subjectEnergyen_US
dc.subjectEngineeringen_US
dc.subjectEnvironmental Scienceen_US
dc.titleTRANSFORMER PRODUCTION IMPROVEMENT BY LEAN AND MTM-2 TECHNIQUEen_US
dc.typeJournalen_US
article.title.sourcetitleASEAN Engineering Journalen_US
article.volume12en_US
article.stream.affiliationsChiang Mai Universityen_US
Appears in Collections:CMUL: Journal Articles

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